Safety Incidents OSHA Severe Injury Reports · 2015–2025
3,913,242Inspections Most recent open 2026-07-13 Last loaded 2026-07-17

OSHA Inspection: BEST WELL SERVICES LLC

Planned inspection · Safety discipline

On , OSHA opened a planned safety inspection of BEST WELL SERVICES LLC in THE TERRY #1-10H WELL, SEC 10-10N-6E SEMINOLE COUNTY, SEMINOLE, OK 74818 (NAICS 213112). OSHA activity number 340059344.

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Site address
THE TERRY #1-10H WELL, SEC 10-10N-6E SEMINOLE COUNTY
City
SEMINOLE
State
OK
ZIP
74818
Mailing
PO BOX 457, PRAGUE, OK 74864
Inspection type
Planned (H)
Scope
Partial (B)
Discipline
Safety
Advance notice
No
Union status
B
Opened
Closing conference
Case closed
Last modified
Data loaded
NAICS code
213112
Employees
4
Ownership type
A

3 citations on file for this inspection.

5(a)(1)

Serious Gravity 5 1 instance 1 exposed
Issued
Abate by
Penalty
Initial $4500.00 · Current $2700.00 Reduced
OSH ACT of 1970 Section (5)(a)(1): The employer did not furnish employment and a place of employment which were free from recognized hazards that were causing or likely to cause death or serious physical harm to employees:  Well site:  On or about October 30, 2014, and times prior to, employees were operating a service rig during the removal of a gas/oil well's production string with one employee working from the derrick mounted racking board.  The derrick emergency escape system (the Geronimo) ground anchorage was insufficient.  This exposed the employee to fall hazards.
Recent events (2)
  • — I (S) $2700
  • — Z (S) $4500

5(a)(1)

Serious Gravity 5 4 instances 4 exposed
Issued
Abate by
Penalty
Initial $4500.00 · Current $2700.00 Reduced
OSH ACT of 1970 Section (5)(a)(1): The employer did not furnish employment and a place of employment which were free from recognized hazards that were causing or likely to cause death or serious physical harm to employees:  Well site:  On or about October 30, 2014, and times prior to, employees were operating a service rig during the removal of a gas/oil well down hole electric pump.  The rig racking board guy lines were attached to inadequate ground anchorages and three of the rig guy lines ground terminations did not have the required number of wire rope clips.  This exposed the employees to struck by hazards.
Recent events (2)
  • — I (S) $2700
  • — Z (S) $4500

1910.23 C01

Serious Gravity 1 1 instance 4 exposed
Issued
Penalty
Initial $2700.00 · Current $1620.00 Reduced
29 CFR 1910.23(c)(1): Open-sided floors and/or platforms four feet or more above adjacent floor or ground level were not guarded with standard railings (or equivalent) and toeboards:  Service rig floor:  On or about October 30, 2014, and times prior to, employees and another contractor's employee engaged in the removal of a down hole electric pump with a service rig worked on the rig's unguarded floor.  This exposed the employees to the hazard of falling over four feet.
Recent events (2)
  • — I (S) $1620
  • — Z (S) $2700

View BEST WELL SERVICES LLC's full OSHA safety record →

This record is reproduced from the U.S. Department of Labor Open Data API (OSHA inspection dataset). The original IMIS detail view is available at OSHA's Establishment Search for activity number 340059344.