Safety Incidents OSHA Severe Injury Reports · 2015–2025
2,004,209Inspections Most recent open 2026-07-13 Last loaded 2026-07-17

OSHA Inspection: PARKER GAS COMPANY, INC.

Referral inspection · Safety discipline

On , OSHA opened a referral safety inspection of PARKER GAS COMPANY, INC. in 30313 FM 529, BROOKSHIRE, TX 77423 (NAICS 454310). OSHA activity number 347821282.

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Site address
30313 FM 529
City
BROOKSHIRE
State
TX
ZIP
77423
Mailing
30313 FARM TO MARKET ROAD 529, BROOKSHIRE, TX 77423
Inspection type
Referral (C)
Scope
Partial (B)
Discipline
Safety
Advance notice
No
Union status
B
Opened
Closing conference
Case closed
Last modified
Data loaded
NAICS code
454310
Employees
260
Ownership type
A

8 citations on file for this inspection.

1910.37 B02

Serious Gravity 5 1 instance 24 exposed
Issued
Abate by
Penalty
Initial $9457.00 · Current $5674.00 Reduced

Hazardous substances 2150

29 CFR  1910.37(b)(2): Each exit was not clearly visible and marked by a sign reading "Exit".  On or about October 18, 2024 and at prior times, at the RapidXchange Production Facility in Brookshire, Texas, the doorway on the east facing wall, of the office building, leading to the eastern side of the building and parking lot was not marked by a sign reading "Exit".
Recent events (2)
  • — I (S) $5674.2
  • — Z (S) $9457

1910.119 E01

Serious Gravity 10 1 instance 10 exposed
Issued
Abate by
Penalty
Initial $16550.00 · Current $9930.00 Reduced

Hazardous substances 2150

29 CFR  1910.119(e)(1): The employer did not perform an initial process hazard analysis (hazard evaluation) on processes covered by 29 CFR 1910.119.  (a) On or about October 16, 2024, at the RapidXchange facility in Brookshire, Texas, the employer did not conduct an initial process hazard analysis to address the propane process hazards.
Recent events (2)
  • — I (S) $9930
  • — Z (S) $16550

1910.119 F01

Serious Gravity 10 1 instance 7 exposed
Issued
Abate by
Penalty
Initial $16550.00 · Current $9930.00 Reduced

Hazardous substances 2150

29 CFR  1910.119(f)(1): The employer did not develop and implement written operating procedures that provide clear instructions for safely conducting activities involved in each covered process.    (a) On or about October 16, 2024, at the RapidXchange facility in Brookshire, Texas,  the employer did not implement the propane evacuation of cylinders procedure as written.
Recent events (2)
  • — I (S) $9930
  • — Z (S) $16550

1910.119 J02

Serious Gravity 5 2 instances 8 exposed
Issued
Abate by
Penalty
Initial $11823.00 · Current $7094.00 Reduced
29 CFR  1910.119(j)(2): The employer did not establish written procedures to maintain the ongoing integrity of process equipment:  (a) On October 16, 2024, and at times prior, at the RapidXchange facility in Brookshire, Texas, the employer did not establish written procedures to maintain the ongoing integrity of Pressure Vessel #1 containing 59,220 lbs. of propane.  (b) On October 16, 2024, and at times prior, at the RapidXchange facility in Brookshire, Texas, the employer did not establish written procedures to maintain the ongoing integrity of Pressure Vessel #2  containing 88,992 lbs. of Propane.
Recent events (2)
  • — I (S) $7093.8
  • — Z (S) $11823

1910.119 J04 II

Serious Gravity 5 3 instances 7 exposed
Issued
Abate by
Penalty
Initial $0.00 · Current $0.00
29 CFR  1910.119(j)(4)(ii): Inspection and testing procedures did not follow recognized and generally accepted good engineering practices:   (a)	On October 16, 2024, and at times prior, at the RapidXchange facility in Brookshire, Texas, the employer did not follow Recognized and Generally Acceptable Good Engineering Practices (RAGAGEP) such as but not limited to, API 510 Pressure Vessel Inspection Code: In-service Inspection, Rating, Repair, and Alteration, (2014) section 9.3.4  for external inspections, when they failed to perform an adequate inspection on  Pressure Vessel tank #1 containing 59,220 lbs. of propane.  (b)	On October 16, 2024, and at times prior, at the RapidXchange facility in Brookshire, Texas, the employer did not follow Recognized and Generally Acceptable Good Engineering Practices (RAGAGEP) such as but not limited to, API 510 Pressure Vessel Inspection Code: In-service Inspection, Rating, Repair, and Alteration, (2014) section 9.3.4  for external inspections, when they failed to perform an adequate inspection on Pressure Vessel tank #2 containing 88,992 lbs. of Propane.                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                                   (c)	On October 16, 2024, and at times prior, at the RapidXchange facility in Brookshire, Texas, the employer did not follow Recognized and Generally Acceptable Good Engineering Practices (RAGAGEP) such as but not limited to, API 570 Piping Inspection Code: In-service Inspection, Rating, Repair, and Alteration of Piping Systems (2016) section 6.4 for Visual External Inspections, when it failed to perform adequate inspection on the process piping connected to pressure vessels containing propane.
Recent events (2)
  • — I (S) $0
  • — Z (S) $0

1910.38 C02

Deleted Other-than-serious 1 instance 24 exposed
Issued
Abate by
Penalty
Initial $0.00 · Current $0.00
29 CFR  1910.38(c)(2): Procedures for emergency evacuation, including type of evacuation and exit route assignments were not implemented by the employer.    On or about October 18, 2024, at the RapidXchange Production Facility in Brookshire, TX, the emergency evacuation posters were not hanging in the areas of the production facility where the workers could see and adhere to.
Recent events (2)
  • — I (O) $0
  • — Z (O) $0

1910.38 C04

Deleted Other-than-serious 1 instance 24 exposed
Issued
Abate by
Penalty
Initial $0.00 · Current $0.00

Hazardous substances 2150

29 CFR  1910.38(c)(4): The employer did not establish procedures to account for all employees after an evacuation.  On or about October 16, 2024, at the RapidXchange Production Facility, in Brookshire, TX, the employer did not have a secondary means of establishing accountability after a significant incident.
Recent events (2)
  • — I (O) $0
  • — Z (O) $0

1910.38 D

Deleted Other-than-serious 1 instance 24 exposed
Issued
Abate by
Penalty
Initial $0.00 · Current $0.00
29 CFR 1910.38(d): The employer did not have and maintain an employee alarm system with a distinctive signal for each purpose so that it complied with the requirements of 1910.165.  On or about October 16, 2024, at the RapidXchange Production Facility in Brookshire, Texas, the employer did maintain an alarm system with a distinctive signal for fire or other emergency situations that might occur.
Recent events (2)
  • — I (O) $0
  • — Z (O) $0

This record is reproduced from the U.S. Department of Labor Open Data API (OSHA inspection dataset). The original IMIS detail view is available at OSHA's Establishment Search for activity number 347821282.